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Epilogue - Spider rear wheel bearing



Three weeks ago I whined to the digest that I had a bad rear wheel bearing on my '73 spider, but could not get the brake rotor off to even begin the repair. No amount of heat or pullers were working. I received several responses to my dilemma and a few off-line requests for the solution if/when I effected the repair. Here it is:

Tom and Russ suggested removing the axle and rotor as a unit by removing the 4 bolts that hold the brake backing plate to the axle tube, then use a slide hammer (or equivalent) to remove the axle/rotor (be sure to disconnect the emergency brake cable for that side at the differential mechanism). That solution worked for me, though there was still a bit of effort to pull out the stuck axle. Once off, I still had a very rusted stuck rotor attached to the axle, but had a much better angle of attack for my BFH tool. What finally worked was placing the rotor/axle between two same-height work benches such that the rotor was supported by the work benches but the brake backing plate was in the gap. This allowed the rotor to be supported but not the backing plate (also had the benches in a V configuration to support as much rotor surface as possible). Then I used my Thor brass sledge hammer to wail on the center of the axle hub where it protrudes from the brake rotor. That is a small target, particularly when you are trying to get a full and powerful swing, so be sure to use a hammer softer than the wheel studs when you miss! Or use a hydraulic press...

I had been using liberal amounts of penetrating oil, and finally the rotor began to loosen up and separate. Required LOTS of heavy hits!

The rest of the disassembly was straightforward. I removed the emergency brake shoes by pushing and turning the hold down springs 90 degrees with a 5mm hex, then disconnecting the springs. One of the best tips was from Greg who cautioned to PAY ATTENTION to how the emergency brake was assembled. In particular, the emergency brake cable is attached to an "actuator" that has two small pins that will fall out and could be easily lost.

After I had the emergency brake shoes and hardware removed, I also removed the 4 studs from the backing plate that are used to secure the assembly to the axle tube. These studs and the brake hardware will get in the way of removing the bad wheel bearing. At this point you have the axle with brake backing plate sandwiched between the wheel flange and the wheel bearing.

I took the assembly to my Good Ol' Boy machinist who removed the old retainer and wheel bearing, and replaced the new parts. Took him 15 minutes, and he did it with a BFH and brute force. First he used a stout steel punch about 2" in diameter and the previously mentioned hammer to break the old bearing's outer race by wacking it REAL HARD while it was supported by some steel bars. He also used the same process to hit the retainer few times after which he was able to drive it off. The bearing's inner race was cut with an air tool, whacked a few times and then driven off. Finally he used his hydraulic press to gently push on the new bearing and retainer. Cost me 15 bucks - what a deal!

The wheel bearing was bad. Several digesters cautioned me that these wheel bearings rarely fail, and suggested alternative faults. This bad bearing had one deformed ball bearing, and the inner race was badly scored. Now I know why there was that irregular ticking-taping noise - the bearing cage was getting hung up on the race as the wheel turned. However, the bearing still had lubrication and turned freely, if not smoothly, and did not appear ready for a immanent failure.

//kct, Powell, TN --
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